May  2002


Electrical Problems:

 

After dealing with Murphy and his damn law…

 

The alternator whine, which had returned was corrected by replacing the filter installed back in September /00.  I purchased the original from JC Whitney for around $50 and it worked well until May /02 when it failed.  The replacement is made by American International and is a model S-15A CL.  It also works well, but cost considerably less at the local Canadian Tire store (about $25).

 


 

The Revenge of Murphy:

 

I had only flown about an hour since my last debacle when I noticed another “small problem”…

 

My next run-up showed a noticeable mag drop and some engine roughness on one mag.  Checking the plugs showed them to be clean but it was obvious some arcing had been taking place at one of the lead ends.  This end had already been replaced once and there was insufficient material remaining to repair it again. 

 

Since the remaining leads were showing their age I decided to have a new set made up and have the mag inspected.  I was planning to have this done later this year anyway since the engine was assembled in 1983 and now has about 250 hours.

 

While the mag was off I decided to do a 50-hour inspection.  During this inspection I noticed the exhaust valves on the front cylinders were still closing in and pulled the heads to investigate.

 

What I found were small cracks beginning to form between the valves (a common occurrence in VWs).  It was also obvious the front cylinders were running leaner than the rear ones.  It appeared the valves were sinking into the head (which would explain the gap closing).

 

Rather than repair the old heads I purchased a set of premium heads from Steve Bennett and had them machined for the Revmaster.  I liked the idea of the stainless valves and extra heat dissipation capability of these heads. 

 

While the heads were off I also planned to hone the cylinders and re-ring the pistons.  To this end I enlisted the services of a local engine shop, who it turns out are also familiar with Murphy.

 

Back to Steve Bennett for a set of CIMA 92 x 82 cylinder/pistons,  0.100” shims and a pushrod kit (required since I am using the shims to lower the compression ratio.

 


 

Compression Ratios:

 

My engine was set up for a 9.3 : 1 compression ratio.  Currently Steve Bennett is recommending a maximum of 8.0 : 1.

 

Examination of my old pistons (front) showed signs of detonation (removed material).  The causes of detonation are… too lean a mixture, too low a fuel octane rating or an excessive compression ratio.

 

The full rich mixture was set to about 125 deg F below peak as recommended (measured at number 3 cylinder).  Cylinder head temperatures (again measured at #3) were well within limits in all flight regimes.  It was possible to enrichen this mixture somewhat prior to the onset of engine roughness.

 

Fuel was exclusively 100 low lead.

 

Examination of the plugs/pistons/cylinders suggest the mixture was lean despite the EGT indications.  This may be caused by running the engine at “unfavourable” carb settings.

 

During cruise flight I noticed that operating the engine at full throttle actually gave lower egt and cht readings than at some lower throttle settings.  In fact, reducing power from 3200 RPM to 2900 RPM would noticeably increase EGT and CHT.  This would seem to indicate the needle profile of the carb is not optimum. 

 

When we examine the way we set up the carb I believe we find the answer.

 

One observes the engine reaches full RPM long before the throttle is fully open.  At the max RPM point the carb is flowing as much air as the engine can, however the fuel orifice has not yet reached its maximum size.   As the throttle continues to open the needle is pulled further from the orifice the mixture becomes richer.  Since we are adjusting the carb for full rich mixture at full throttle it seems apparent that the engine will run “lean” in the range of throttle settings between max RPM point and full open. 

 

I plan to move the EGT probe to #4 cylinder (front) and adjust the full rich mixture to 175 deg F below peak.  This combined with my reduced compression ratio (7.6 :1) should greatly reduce the stress on the engine and extend its service life.


Trim:

 

After nearly 2 years flying it was high time to get rid of the “flying dishwasher” look.  It was also apparent that The Gadget was hard for other pilots to spot and needed some colour to aid in visibility.

 

The trim is basic automotive enamel (spray bomb).  Masking was done with 3M Fine Line tape.  This stuff is worth the extra money.  Regular masking tape will not give a consistently clean edge.  The procedure is straight out of Bingelis.

 

Lettering and logos were obtained from a local sign shop. Applying vinyl is really quite easy and had the fuselage stripes in my design been of equal width I would much rather have used vinyl here as well. 

 

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Inside of the canopy and turtledeck was painted with a simulated stone type paint and sealed with the recommended clear coat.  To date it has proved reasonably durable.

 

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